Mixed feelings after working on things tonight…
Started off pretty well by pulling some expansion plugs and washing gunk out of the block! PO left water in the block for the 5 years he had it disassembled, I guess he didn’t know about the drain in the block? Here's what it looked like when I started

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And here’s the video of the first gunk out of the block:
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https://youtu.be/HGpklk87Hjs?si=UJhoIM5h-O0jgoHD[/youtube] (can’t get the video to imbed, which tag am I supposed to use? Is it because I’m on my phone?)
After lots of rinsing, poking around with a coat hangar (and deciding half way through that taping the top of the block was a good idea - Gorilla tape for future reference) it’s currently at this point:
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Still some cleanup needed on the cylinder walls, I think I’m going to seal up the expansion holes with tape or maybe some of the rubber expansion plugs and then soak the while thing in vinegar for a few days. There’s also some bridging between cylinders, I’m not sure if it’s casting material or scale that’s just really wedged in place. I think the vinegar soak will clarify that some.
Once I’d gotten things dried off I chased all the holes for the head bolts, looooots of gunk in the bottoms, like seriously, where did this all come from?!
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I also chased the threads on the head bolts, and this is where the night started getting rough. All the bolts bound up at some point on the die, after examining them all a bit I’m pretty sure the threads have yielded to some extent on all of them. So I’ll need new bolts or studs… Disappointing since I’m really just doing this so I can get it registered with a bonded title here in Tx, and was hoping to get some days of driving it before I started in on engine swap and real restoration/mod. So now spending more money on an engine I’m not using for long.
I did a quick visual check of the distributor timing and it looks good, it could be off by a tooth I guess but I don’t think I can tell that at this stage?
I then moved on to some clearance checks between head and pistons because the head seemed really thin. I put some playdough on the pistons and snugged the head down with a few of the bolts, found a hole that needs more work, yay! I didn’t install the head gasket because I figured there should be at least that much clearance?
Anyway, I turned the engine over slowly and hit a point where it wouldn’t turn any further no matter how much I tried. So I backed the head bolts off a few turns thinking it could be compression since I didn’t have much leverage and I don’t have the rocker arms installed. That didn’t end up helping so I took the head off haha. This is what I found on the piston side

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I didn’t get a pic of the head but there was more dough mashed on #3. Looked an awful lot like contact so i cleaned up the playdough and just set the head on top of the block to see what happened. Got contact on both pairs of cylinders!

After that I went ahead and measured the head thickness, which I should have done first! It measures out at about 3.11” so .078” lower than minimum allowable according to:
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I made a very unscientific set of shims out of folded paper towels, measured out to about .045” with the calipers but I suspect was closer to .060” since the head didn’t apply as much pressure. Didn’t get any contact with that setup. I’m bummed, already ordered a standard head gasket but now at the very least I need to get a thicker one. Or find a different head (donor car might save me here). Or work on the dish in this head (anyone know how much material is there before I hit water passages?)
I decided to call it quits at that point, now I’m drowning my troubles in good Scotch, ending the night on something nice!
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PS. Yesterday was a good day, I got the carbs all back together and happy (except for the overflow tubes) Turned out the oxidation from the Krud Kutter cleaned piston/dome was enough to slow the piston significantly. I guess if you need to add back material that’s a method! I did some work with a scotchbright pad and now both pistons are almost perfectly in sync.
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