I've been working on many different projects. Usually multiple projects at once. I'll try and list the projects in order from oldest to most recent. I actually just recently started another fun project that RustBucket actually has been helping me with since he had the same issue last year.
Get on with it! Bring on the pictures!
First picture I wanted to show is where I work on the Datsun. We don’t have garages in my complex. I also have to clean everything up by the end of the night. This is why projects take me a lot longer to complete.
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Changed fuel filter. Cut old filter open to inspect how bad it was. It was bad. Changed to a see thru filter case
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Temporarily fixed the exhaust hole with exhaust tape. Future project will be entire new exhaust system.
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Bought new door locks. Had to file them down a little to make them fit in the door. Driver side are in door now but I haven’t attached the arm yet.
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Removed driver side pieces to clean and polish. Sorry I don’t have a finished picture. I will take better pictures when I do the passenger side.
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While driving down PCH (Pacific Coast Highway) my starter kicked on which was followed by smoke coming from my dash. Immediately pulled over and had it towed home. An ignition wire was fried. The ignition switch was also fried and it appeared a prong was loose too.
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Bought new ignition lock and switch assembly. Tried to install but the diameter of ignition bracket that goes around the steering wheel was too large. Found out there are actually two different sizes. Returned and bought correct size.
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Messaged Steve about the tech wiki page on the ignition alternative. Asked if we could add the correct size that should be bought along with a picture showing which wire goes to the correct prong on the switch. The diagrams are great but they still did not show the actual prong location. I edited a few pictures I took and sent them to him. Wiki page was edited with kudos from Steve. Thanks Steve!
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Bought a new alternator. Still need to install but first I need to cut my bracket to make it fit.
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One day heard a “pinging†sound that appeared to be coming from cylinder 3 or 4. Took a brief video and sent it to some local 311 members. They said valves seem to need to be adjusted. Began the process to measure valve slash. Tried cranking engine but had trouble reaching the crankshaft nut.
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Removed fan shroud to make more room and still had an issue reaching it so I then removed the fan too.
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Removed plugs. Got engine to TDC. Feeler gauges ready. Time to measure them all.
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Cranked and cranked till I felt like Popeye. Made a note on which valves appeared to not meet the .017 measurement. Red circle was too tight and blue circle was too loose.
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I then was ready to proceed with now making the slight adjustments. I get the socket on the locking nut on the tower to loosen it. It would not budge. I thought I was doing something wrong. Researched… messaged 311 members again… it was correct. This was just extremely tight. Finally got it loose while smacking my arm on the car in the process. Cylinder 1 done. On to cylinder 3. Back to the crank.
Cylinder 3 “done†and I begin to lock it back in place. It keeps spinning but not getting tighter. I then hear a compression leak sound and realize the tower was rising while I was tightening and that’s why it was not getting tighter. This then forces me to remove the entire camshaft, towers, arms, etc to figure out what happened.
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The 2 middle studs were stripped. You can see in the pic the #3 cylinder stud and how far out it came. I then removed these studs to inspect further.
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One stud came out with the aluminum perfectly wrapped around it. The other didn’t have any aluminum on it but when I looked down the stud hole I saw what appeared to be helicoil… looks like this wasn’t the first time this happened.
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Decided to clean the area and rods while I was there. Pulled rod, cleaned, and inspected. Sure enough found the #3 cylinder intake rod had markings along the bottom from hitting against the wall (I believe)
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Still haven’t fixed the stud issue. I’m nervous about beginning the drilling and helicoil process. So in the meantime while I wrap my head around it I decided to clean up and polish the valve cover and some rusted valve cover grommets and air filter locks.
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I have another project but I don’t want to post anything on it until it is complete.
Well that’s pretty much it. So I will end with a nice picture I took a few weeks ago at the Segerstrom Hall in Costa Mesa.
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